
02-22-2010
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Tundra Down
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Join Date: Jan 2008
Location: Seal Harbor, Maine
Posts: 417
Rep Power: 5
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I suspect NO blockage now. I will have a new exhaust from the manifold to the transom. I wish I had a record of the back pressure for the past year prior to my hot pipe's failure. It would have been an interesting and useful bit of data. My hot pipe failed, cracked open, on a run of about 5 miles which killed the engine. I was aware of the decline once it started to fail completely but I was underway. 20 knots on the nose, declining power, weak exhaust exit, exhaust in the engine space and finally it quit. Fortunately I had just made it to the inlet which was my destination. I radioed for assistance. The wind was blowing past the end of the inlet and I was able to use the dinghy to tow the boat toward its berth. Another boat responded to my radio call and helped me to my float. I replaced the engine 20 engine hours prior to failure. It was well wrapped and there were no outward signs of failure. It was old. I was surprised to see how obstructed the exhaust passage was when I removed the hot pipe and got a look.
All is well now. I did get the engine running before I put it away for the winter. I managed to winterize it properly and expect no problems this spring. I will have a new hot pipe, muffler and exhaust hose. I expect different performance from the engine. It will be interesting to see how much things change. There must have been considerable back pressure from the looks of the inside of the pipe. It went from a high back pressure condition to zero in about an hour. I think for the few bucks I will install the gauge just for the information. I am installing a tach, too. It will provide a new baseline for the next owner I suppose.
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